何杰, 辛文杰. 港珠澳大桥沉管隧道基槽异常回淤分析与数值模拟[J]. 水科学进展, 2019, 30(6): 823-833. DOI: 10.14042/j.cnki.32.1309.2019.06.006
引用本文: 何杰, 辛文杰. 港珠澳大桥沉管隧道基槽异常回淤分析与数值模拟[J]. 水科学进展, 2019, 30(6): 823-833. DOI: 10.14042/j.cnki.32.1309.2019.06.006
HE Jie, XIN Wenjie. Analysis and numerical simulation of abnormal siltation in foundation trench of immersed tube tunnel of Hongkong-Zhuhai-Macao Bridge[J]. Advances in Water Science, 2019, 30(6): 823-833. DOI: 10.14042/j.cnki.32.1309.2019.06.006
Citation: HE Jie, XIN Wenjie. Analysis and numerical simulation of abnormal siltation in foundation trench of immersed tube tunnel of Hongkong-Zhuhai-Macao Bridge[J]. Advances in Water Science, 2019, 30(6): 823-833. DOI: 10.14042/j.cnki.32.1309.2019.06.006

港珠澳大桥沉管隧道基槽异常回淤分析与数值模拟

Analysis and numerical simulation of abnormal siltation in foundation trench of immersed tube tunnel of Hongkong-Zhuhai-Macao Bridge

  • 摘要: 港珠澳大桥沉管隧道E15管节基槽发生异常回淤,海底隧道沉管安装被迫中止。为查明E15管节基槽发生异常回淤的原因,先后开展了现场水文泥沙观测、遥感影像资料分析和数值模拟等多种技术手段。采用水沙数学模型反演了内伶仃岛上游采砂活动形成的浑水团在潮流作用下的扩散输移过程,沙源在数学模型中以面源形式模拟。模拟结果表明,采砂活动形成的浑水团在一个大潮期间的落潮过程中可输移扩散至基槽水域,其中E15—E27管节基槽日淤厚在采砂活动影响下将增加43.8%。数值模拟结果为查明E15管节基槽异常回淤的泥沙来源提供了佐证。E15管节以东基槽水域水沙环境复杂,天然淤积已经接近临界回淤允许值,基槽上游水域的采砂活动对沉管基槽回淤将带来不可控因素,采砂活动对周边水域产生的泥沙回淤影响应引起足够重视。

     

    Abstract: The abnormal siltation was present in the E15 foundation trench of the immersed tube tunnel of the Hong Kong-Zhuhai-Macao Bridge,and the installation of the immersed pipe of the submarine tunnel was forced to paused. In order to find out the cause of abnormal silting at the E15 foundation trench,various technical means such as field hydrological and sediment observation,remote sensing image data analysis and numerical simulation have been carried out. In this paper,the water-sand mathematical model is adopted to simulate the diffusion and transport process of the muddy water mass formed by sand mining activities in the upper reaches of Neilingding Island under the action of tidal current,in which the sand source is simulated in the form of surface source. The simulation results show that the muddy water mass formed by sand mining activities can be transported and spread to the foundation trench during the ebb tide of a spring tide,and the daily silt thickness of the E15-E27 foundation trench will be increased by 43.8% under the influence of sand mining activities. The results of numerical simulation provide evidence for finding out the sediment source of abnormal silting in E15 foundation trench. The water and sediment environment in the east of E15 pipe section is complicated. The natural siltation is close to the critical siltation allowable value. The sand mining activity in the upstream water of the foundation trench will bring uncontrollable factors to the siltation at the foundation trench. Therefore,the attention should be paid to the influence of sand mining activities on sediment deposition in surrounding water area.

     

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